Another day of work on the AC…
* Tightened offside hub onto axle
* Replaced alternator mounting bolts
* Checked and tightened lower engine coolant house
* Adjusted bonnet stop to prevent rattle
* Checked speedometer cable and prepared for removal
* Checked gearbox linkage seal
It occurred to me that I should keep track of things I do to my cars. Typically I’ve done most of the work to the Landie over the past 2 years, and now it’s just minor fixes, but here goes..
* Replaced oil pressure sensor
* Replaced alternator bracket
* Replaced alternator
* Replaced rear fog lamp (thank you Kenny!)
* Re-fitted handbrake expander spring
* Cleaned rear suspension wishbones
[flickr id=”6796206814″ thumbnail=”small” overlay=”true” size=”large” group=”” align=”left”] Recently I had the misfortunate to wear out my alternator. It started under-charging, and my battery would slowly discharge over the course of a week. It was time for a replacement. This would normally be a routine task, if it weren’t for a massive potentially £200 gotcha that seems to befall a few of us.
The Series 3 originally comes with a 28Amp Lucas 16ACR alternator, and this is mostly superceded by the 17ACR – a drop-in 35A replacement that everybody seems to use. Well, it’s mostly drop in…
[flickr id=”6796205110″ thumbnail=”small” overlay=”true” size=”medium” group=”” align=”right”]I found out the hard way, when the new alternator chewed through a fan belt in under 20 miles. Further inspection showed that the alternator pulley was about 6mm further forward than on the previous alternator. Much searching on Google revealed that in the cases of those with engine numbers starting 901, 904, 361 or 364, with suffix A or B, a bracket is required. Specifically part ETC4357 or 574855. Everywhere you search for this part will offer it for the best part of £200. If you’re unsure what your engine number is, look on the left hand side of the block, just behind the face that the water pump mounts on, and just below the first exhaust port. Scrub it clean, wedge your head into the engine bay, and get the number. A list of prefix and types can be found at http://www.glencoyne.co.uk/engno.htm if you’re also interested.
[flickr id=”6942321385″ thumbnail=”small” overlay=”true” size=”large” group=”” align=”left”] Unsure about where to go from here, at 9.30pm I got in touch with Dom at LR Series, who replied within 15 minutes. Talk about customer service! He advised that a second hand part is available at a much lower cost if you order it on their website and let them quote for the part. Suffice to say, not only was the part much *much* cheaper, it was also express couriered up and will be at home in less than 24 hours. This, your honour, is the solution to the bracket-for-slightly-less-common-engines problem, and how you make loyal customers 🙂
As has been noted earlier, the AC has had its fair share of fuel flow problems. Ranging from the large (a rotten fuel tank) to the tiny (a flake of corrosion in the accelerator pump). Here’s a few things that were done to try and cure it.
Firstly, replace the filters that sit on top of the fuel tank drain plugs. They may not seem like much, but internally the fuel intakes come down inside the tank, and slip inside the filters that are on top of the plugs. This fine mesh is the first line of defence against rubbish in the fuel tank. We thought we could get away with old ones that had a slight tear in them. After a few weekends of running, further inspection showed a pile of gunk sitting inside the filter! This would lead directly to the fuel pump…
The second thing to do was to insert an inline filter between the fuel solenoid (since the AC has two fuel intakes), and the fuel pump. This is just a bog standard plastic inline fuel filter after the solenoid, and is there to save the pump from any rubbish that somehow gets past the gauze filters on the drain plugs. We also took the chance to replace all the fuel hoses between the solenoid and the carburettor. The existing hoses were coming up on 30 years old, so we though it wise to avoid any rubber degradation issues and replace the whole lot in one go.
Roughly at the mid-point now, we opted to change the fuel pump. It had been noted that the fuel was flowing back down the line after the car had been left to sit for a day or two. This made starting it particularly difficult, and was probably the precursor to a failed pump. Add to that all the rubbish that had been coming through the fuel system in those weeks of diagnosis, the pump filter had been cleaned out more often then we had had hot meals. A new pump was fitted, and the fuel draining problem immediately vanished.
Annoyingly though, we were still experiencing problems with fuel flow. Between Gordon and I, we must have stripped the about 20 times. Every time it would work great for 20, maybe 50, miles before reverting to its normal way of not letting any fuel flow when under load.
Convinced it was a problem of more rubbish in the fuel system, we decided to fit another filter after the pump and before the carburettor. Initially we went for the cheap plastic inline filters that are readily available, but we didn’t leave it in that configuration for very long for another reason – we fitted a Filter King instead.
The Filter King not only acts as a filter, but it also has a sedimentation bowl which doubles as a small fuel reserve. Any rubbish floating in the fuel can fall to the bottom of the bowl whilst the fuel in the bowl can continue to be drawn upon by the carburettor. We initially tried the Filter King before the fuel pump, but it’s clearly designed to have fuel pushed through it. The pump couldn’t draw air hard enough to draw fuel into the Filter King, and nothing worked. Now, the AC 3000ME range historically has a problem of fuel starvation during a long corner. This is most likely due to the shape of the fuel tank, but appears to be mostly mitigated by the Filter King now.
Sadly, after all this work, the fuel was still not flowing as planned. At higher revs after 30 minutes of running it would start to cut out. Something was clearly wrong, and all things started to point to the carburettor… no matter how many times we stripped it down and rebuilt it!
When you blip the throttle on the AC, it activates the accelerator pump. This pumps a higher than normal amount of fuel into the carburettor in order to rapidly increase the revs of the engine. It also ensures the engine stays running and doesn’t cough and splutter to a halt. Sound familiar? After much poking and prodding, I discovered that the one of the two accelerator pump outlets was partially blocked! These outlets start at about 4mm across, and narrow to about 0.5mm. That’s why it had passed our cursory blowing through the thing to see if it was clear. Using a small length of wire from the fuel hosing braiding, the passageway was cleared, and tiny flake of white aluminium corrosion fell out…
So that was it, all those problems were caused by a tiny bit of corrosion that had worked itself up to the narrowest gap it could wedge itself into. Although it seems like we were on a wild goose chase for a lot of it, I believe that a lot of worthwhile work was still completed. Replacing the drain plug filters was definitely required, the pump was on the way out, and the Filter King cures some edge case starvation problems, as well as providing a handy visual indicator for the state of fuel flow in the system.